some RF boards might have issues with the sharp filters that are needed
for the reduced sample rate operation that we use by default.
This switch allows to use the default LTE sampling rates and
configure this at run-time, not compile time.
this potentially fixes the issue we see during HO and RLF
under high DL load.
The issue happens because buffered DL PDUs are delivered to
RLC after reestablishing RLC that confuse the receiving
RLC entity bc the sequence numbers are very high, as opposed
to begin with zero again after reestablishment.
* mac_test: add extended TBSR unit test
unit test to MAC UL packing after sending a TBSR
this fixes the MAC issues described in issue #2002
* mux: fix updating of LCG buffer state after packing PDU
we've previously lowered the buffer state of the LCG according
to the bytes that have been scheduled, but not according to
those that have been actually included in the PDU.
* proc_bsr: fix LCG buffer state updating for TBSR
when sending a TBSR do not update the internal buffer
state of the BSR proc.
This caused issues because the buffer state for all LCG that
are not included in the TBSR are set to zero, although at least
one LCG does have data to transmit.
* rlc_am: include LCID when logging retx of SN
the current implementation was somehow broken after a
NAS refactor. It was undetected because we didn't really
use it.
this fixes the simulation by using a single timer to simulate
airplane mode transitions.
the timer is rearmed in the timer_expire() function
if the correspondig event is set.
Has been tested to work well with, e.g.:
--sim.airplane_t_on_ms 5000 --sim.airplane_t_off_ms 10000
fix for #1934
This fixes a race condition between Stack thread and DL
PDU processing that lead to updates of the RLC buffer that
are undetected by the BSR routine.
What happens is that in a UL SCH PDU all outstanding data is transmitted
and and a LBSR with all zero buffers is sent.
14:39:47.327301 [MAC ] [D] [ 3793] BSR: LCID=3 old_buffer=59
14:39:47.330600 [MAC ] [I] [ 3793] UL LCID=3 len=58 LBSR: b=0 0 0 0
Note that "old_buffer" isn't set to zero here.
At the same time (same TTI), the MAC PDU processing thread handles DL-SCH PDUs
that may generate new UL PDUs:
14:39:47.330749 [RLC ] [I] DRB1 Tx SDU (54 B, tx_sdu_queue_len=1)
14:39:47.330762 [RLC ] [I] DRB1 Tx SDU (54 B, tx_sdu_queue_len=2)
14:39:47.330775 [RLC ] [I] DRB1 Tx SDU (54 B, tx_sdu_queue_len=3)
..
Those PDUs are "new data" since the previous buffer state was zero.
Here is the race now between the threads, at the end of the bsr::step() function
old_buffer of each LCG is updated with the previous new_buffer, so
the buffer state of LCG=2 is now 59.
Now MAC starts the next TTI:
14:39:47.331910 [MAC ] [D] [ 3794] Running MAC tti=3794
14:39:47.331928 [MAC ] [D] [ 3794] Update Bj: lcid=0, Bj=0
14:39:47.331934 [MAC ] [D] [ 3794] Update Bj: lcid=1, Bj=0
14:39:47.331938 [MAC ] [D] [ 3794] Update Bj: lcid=2, Bj=0
14:39:47.331941 [MAC ] [D] [ 3794] Update Bj: lcid=3, Bj=-1752
14:39:47.331951 [MAC ] [D] [ 3794] BSR: LCID=0 update new buffer=0
14:39:47.331960 [MAC ] [D] [ 3794] BSR: LCID=1 update new buffer=0
14:39:47.331964 [MAC ] [D] [ 3794] BSR: LCID=2 update new buffer=0
14:39:47.331971 [MAC ] [D] [ 3794] BSR: LCID=3 update new buffer=335
14:39:47.331976 [MAC ] [D] [ 3794] BSR: check_new_data() -> get_buffer_state_lcg(0)=0
14:39:47.331980 [MAC ] [D] [ 3794] BSR: check_new_data() -> get_buffer_state_lcg(1)=0
14:39:47.331984 [MAC ] [D] [ 3794] BSR: check_new_data() -> get_buffer_state_lcg(2)=59
14:39:47.331988 [MAC ] [D] [ 3794] BSR: check_new_data() -> get_buffer_state_lcg(3)=0
14:39:47.331993 [MAC ] [D] [ 3794] BSR: LCID=0 old_buffer=0
14:39:47.332000 [MAC ] [D] [ 3794] BSR: LCID=1 old_buffer=0
14:39:47.332003 [MAC ] [D] [ 3794] BSR: LCID=2 old_buffer=0
14:39:47.332007 [MAC ] [D] [ 3794] BSR: LCID=3 old_buffer=335
And since the buffer state of LCG=2 isn't zero, the new data for LCID=3 of that LCG is considered.
So effectivly, the BSR missed the "empty" buffer state for a fraction of time and doesn't
consider the outgoing data generated in the same TTI as new. It therefore
doesn't transmit a BSR.
in which a BSR wasn't
this was a very noisy log that was printed in pretty much
every TTI because the BSR procedure starts a SR whenever
it needs to send a regular BSR. The SR is canceled when a UL
grant arrives but the log line stays there.
Since we are printing a log when we actually signal a SR
to the PHY, this line is not needed.
this fixes the trigger logic for periodic BSRs. Previously we
would always trigger the "new data for highest priority LCID"
whenever new data becomes available for a LCID for which
a BSR has already been sent.
However, a BSR should only be sent if the priority is in fact higher
(lower int number).
the BSR routine had a bug in which it would generate a BSR even
before the reTx timer expires if new data becomes availble
for a LCID that already had data and a BSR was already sent.
The RA test here relies on a BSR in the generated MAC PDU to pass.
However, since after fixing the BSR bug the PDU the MUX unit
no longer generates a BSR, we need generate data for a LCID
which has higher priority than the one for which a BSR has
already been sent.
in ZMQ runs we've seen that entering idle could take quite
a bit of time depending how quickly workers get their samples
sent or reconfigurations done.
In one example up to ~160ms
this patch increases the maximum wait time to 2s.
the BSR trigger wasn't reset after includinga regular or periodic
BSR inside a PDU. This caused the muxing to include another BSR in the
next UL grant. For very small grants, for example with 6 PRBs, this
causes the UE to send way too many BSRs.
this test varifies the correct operation of the retxBSR timer.
the first PDU includes a long BSR to indicate more LCGs have
data to transmit. The retxBSR timer is started and subsequent
PDUs should not send a regular BSR.
After the retxBSR timer expires, a UL PDU should again include
a BSR.
when releasing PUCCH/SRS (see 5.3.13 in 36.331) we need to reset the SR config as well.
In our case, SR is handled by MAC so we need to (re-)configure MAC, not all of
MAC though, just SR.
this avoid logging a warning on UE shutdown if the MAC is already reset
but one of the PHY workers still decodes an UL grant for the old RTNI
21:30:29.254844 [RRC ] [I] Going RRC_IDLE
21:30:29.254848 [RRC ] [I] Proc "Go Idle" - Left connected state
21:30:29.259499 [PHY0] [I] [ 3865] Finished setting new PHY configuration cc_idx=0
21:30:29.259512 [PHY0] [I] [ 3865] Setting new PHY configuration cc_idx=0...
21:30:29.264190 [PHY0] [I] [ 3867] Finished setting new PHY configuration cc_idx=0
21:30:29.275036 [PHY1] [I] [ 3872] PHICH: hi=1, corr=1.0, I_lowest=1, n_dmrs=0, I_phich=0
21:30:29.275050 [MAC ] [W] [ 3872] Received grant for unknown rnti=0x46
this fixes issue #1846 that appears to be related
to the enter/exit state for measurements that is kept
even after a cell disappears from the neighbor list
this fixes#1791 which was caused by a race between
the PHY workers preparing a new UL-SCH PDU and the Stack resetting
the MAC, which in turn resets the HARQ processeses, which cleared
the buffer and set the length to zero.
Not explicitly clearing the buffer on a HARQ reset seems to be
fine since the PHY worker clears the buffer before starting to
pack a new PDU anyway.
The “IPv4 local address type” filter should be 9 bytes since it includes
not only the ip address, but also its subnet mask.
Quoting from 3GPP TS 24.008 10.5.6.12:
"""
For "IPv4 remote address type", the packet filter component value field
shall be encoded as a sequence of a four octet IPv4 address field and a
four octet IPv4 address mask field. The IPv4 address field shall be
transmitted first. For "IPv4 local address type", the packet filter
component value field shall be encoded as defined for "IPv4 remote
address type".
"""
Same for the ToS which also includes a 1 byte mask value
* Fix deadlock caused by update_measurements calling in_sync
* Fix overlapping SRS condition
* Do not use shortened PUSCH in transmissions and retx from RAR
* Revert "Fix deadlock caused by update_measurements calling in_sync"
This reverts commit f58c8c8c766f8f95baa3a3bf8287d8e25b2057ba.
* Take into account CRS from neigbhour cells when measuring interference
* fix std::isnormal compilation
* Fixed compilation of test
* Address comments
* Remove unused overrides
* Make PHY non-blocking and fefactor HO procedure
* makes entire PHY non-blocking through command interface
* adds dedicated queue for cell_search/cell_select commands
* refactor HO procedure to run faster, in one stack cycle. Looks closer to the specs
* force ue to always apply SIB2 configuration during reestablishment
* Run update_measurements in all workers
Co-authored-by: Ismael Gomez <ismagom@gmail.com>
this was preventing that the Temp-CRNTI used in the RAR to be identical
to the currently configured C-RNTI of the UE.
The issue simply was that the RACH procedure was declared successful too
early, even before the Msg3 UL grant was filled with the Msg3 content.
The patch moves the logic that detects the successful completion of
the RACH procedure below the Msg3 packing.
* Removed magic numbers.
* Reduced indentation of statements with early exists.
* Removed elses after a return statement.
* Trimmed unnecessary include files.
* Default initialized members in the class.